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Anyone out there had any experience skimming of the head of an M30 engine in order to raise compression ratio from 9:1 up to 10:1 ?
632 Regal
01-26-2005, 04:13 PM
wow.
Hi Jose,
Did you manage to find any more useful information with respect to your question?
Were you planning to run 10:1 with the standard cam or with a longer duration one? A longer duration cam should drop the effective compression ratio, so you can, in theory, get away with more static compression. :)
Martin in Bellevue
03-03-2005, 11:02 AM
would throw the cam timing out the window.
Hi Jose,
Did you manage to find any more useful information with respect to your question?
Were you planning to run 10:1 with the standard cam or with a longer duration one? A longer duration cam should drop the effective compression ratio, so you can, in theory, get away with more static compression. :)
Hi Martin,
Emmissions could certainly be an issue, depending on your locality.
I would assume that the available fuel octane would also have been taken into consideration before such changes were implemented. :)
Cam timing could be sorted out reasonably easily, and you would expect it to be addressed on any engine being changed that much.
My quick calculations worked out that for a 0.010" skim you would see a 0.26 degree advance in cam timing. Another quick calc reckons on needing a 0.044 thou skim to obtain a 9.99:1 CR assuming the motor started off as spot on 9:1. A 0.044" skim would advance the timing by 1.15 degrees. Assuming I haven't messed up the calcs too much, the cam timing adjustment required is not that big. In fact, assuming no interference issues, a slightly advanced cam would, as I understand it, tend to help improve bottom end and midrange power at the expense of a small bit of top end. :)
I would also assume that valve drop clearance would also have been addressed in such a build, especially if the cam in use is running a higher lift as well as longer duration.
I would also assume that the engine management would be remapped to properly manage the new configuration. :)
Personally, I like the idea of a higher than 9:1 CR M30B35. Alpina ran a hotter cam and a 9.5:1 CR in the B10 non-turbo car. This car made more power than the factory 535 and, as I understand it, returned better fuel economy too. The throttle response woulld also benefit from higher compression. :) I suspect that the B10 non-turbo also had to pass exactly the same emmissions standards that the factory 535 would have.
So, other than cam timing, internal clearances, fuel octane, and emmissions issues, what are the other big issues that need to be considered when running more than 9:1 CR on an M30B35 motor?
Cheers.
msm
Martin in Bellevue
03-03-2005, 12:33 PM
I have the Ireland 284 regrind in my '89 535. It has a little something; Ireland offers a 292 which would require oversized eccentrics. It would seem to be what you are looking for, at a hella good price. https://secure9.nexternal.com/shared/StoreFront/default.asp?CS=ireland&BusType=BtoC&Count1=937755763&Count2=854896187
I think custom pistons would be the way to higher compression. There was a set of m88 pistons on ebay recently that a few of us were watching; I question the wisdom of a rebuild with used pistons, but they looked very good in the auction. Most bmw tuners/rebuilders want at least $1,200 for a set of high compression pistons.
I do agree that more compression should really wake up the m30.
Hi Martin,
Thanks for the recommendations. :) However, I am currently in the process of sorting a failed headgasket, and I have already replaced the worn cam and associated bits. With any luck, I may get the chance to put the head back on this weekend.
I was actually interested to expand on the discussion of running higher compression on the M30B35, as there doesn't seem to be very much in the way of technical information about this on the forum as yet. Personally, I feel that 10:1 from a skim is pushing it a bit far, however, I cannot see why ~9.5:1 (through a skim) would necessarily cause massive problems, assuming, of course, it is balanced with appropriate supporting changes.
msm
Craig
03-03-2005, 03:14 PM
I do agree that more compression should really wake up the m30.
I got yer compression right here! :p
http://www.535i.net/random/BMW/turbo/DSCN1338.JPG
Seriously though, from what I've seen on dynos and heard anecdotally it's pretty damn hard to get much more power NA from an M30.
A point higher compression will yield about 4% more power, or maybe 10hp on the high end. That's not much, for a lot of work and money. You'd see similar gains with just a MAF conversion, with a lot less work and money. Even throwing the kitchen sink at the car (MAF, head, cams, etc) would probably not get you much more than 240-250hp, at least based on what I'd seen from this board and local cars.
Skimmed it 0.65 mm with a 288 degree cam Omega forged pistons custom headgasket , tubular manifold, de-catted it, open HKS Skyline muffler and chipped the hell out of it. Nothing more than 254 bhp at the wheels. Just crap if you ask me.After cranking it every day to see if it would hold, the head cracked in 5 places after only 600 miles.
That made me decide to just build a whoop-ass turbo M5 slaying machine. No more fussing about with the M30 engine, it's a torque motor not a revs machine.It will never be real fast if you don't turbo it. If you don't believe,read this; 9 of our customers have E30 M3's of which one is a rare Alpina M3 B6 3.5s with 260 bhp. This thing is not quicker then a standard M3, just because it takes too long to rev. Turbo is the solution for real power.
Craig,
LOL! :)
Good point about forced induction, however, in my case, I already have a silly fast turbo car as a toy, I bought my 535 as the sensible grown up car to rely on whatever state I leave my turbo car in. I am currently building an experimental engine up for the toy, so the 535 seemd a good idea (used to have an E30 M3 for the same reasons). Naturally, the 535 decided to spit out its headgasket before the new engine for the toy was finished. Such is life. :)
Anyways, I wanted a decent sized NA motor with RWD to play with and to help with my M3 withdrawal symptoms. :) I want to keep it NA and enjoy the good points of NA motors. :) I have enough fun playing around with turbo lag and suchlike on the toy.
Jose,
I'm sorry to hear that the NA tune didn't last long for you. How high a compression did you end up running on it? An instantly responding non laggy 254hp at the wheels must have been pretty impressive, at least for a while.
msm
632 Regal
03-03-2005, 09:20 PM
the reason I first just said "wow" is that that sounded like a lot of skimming, about .040 thou. I did it lots on Detroit iron with minimal pitfalls but as to aluminum on iron or aluminum on aluminum I havent read much of anything on it, even in racing circles.
Id guess going to 10:1 compression from 9 wouldnt actually be a big deal, the motronic regulates fuel and stuff and would probably equate to more mileage but as to power id guess the gains would be minimal to none.
My personal experience to something would be close to an old Kawasaki 900 I had. First thing I did was pop in 10:1 pistons (larger bore) and resize it to appx 1075cc...minimal gain. Next addition was a "hot" ignition...again NO gain. Next was smoothbore larger carburetors...minimal if at all in gain. Next was a Kirker headder...zip. Next was Andrews 2x cams (just one step above stock) WHAM! just like a turbo was installed! Everything else was done and perfect for the cams and the gains but I did it all backwards and didnt see any improvement till I was done.
I dont believe compression alone will make enough difference for anyone to even mention on a project such as yours, thats saying that taking that much material off the head wont cause any weakness. .040 is a LOT concidering piston quench areas and valve to piston clearance, just the quench area alone will cause a dramatic difference in emmisions and spark knock (detonation). One example is the big block chevy engine, had closed chambers with 10.25:1. In the early 70s from the governments self proclaimed energy crisis the auto industry dropped compression ratios down to 8:1-8.5:1, in this particular engine it picked up almost 70 HP. Some of the reasons equate to the unshrouding of the valves, a greater quench area and a more free breathing cylinder face for more flow even though the compression dropped almost 2 points.
I have no idea why I got into this besides the fact that compression in itself with no other changes wont make much of a notisable difference...I think.
To be honest, I too don't think you will get any large number of bhp increase by raisinig the compression, you will just gain on throttle response . BHP increase would be no more than 2-3 hp. As for valve clearence, there's enough room in the M30 engine to experiment with skimming, just as long as you remember to fit stronger valve springs ( schrick for instance ) If you don't experiment with your engines, you will never know the true limits of its capabillity. That's what makes experimenting so much fun. After all,it's just an M30 engine, I wouldn't take my chances on an engine like yours, way too expensive for me if it decides to puff the magic dragon!!!
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